Fallo estructural fatal durante el lanzamiento por torno del SZD 24-4A Foka 4 en el aeródromo de Bicester

Bicester Airfield, Oxfordshire, United Kingdom SZD 24-4A Foka 4

El 8 de agosto de 2010, un SZD 24-4A Foka 4 experimentó un fallo estructural catastrófico durante un lanzamiento por torno en el aeródromo de Bicester, Oxfordshire. Las alas se separaron del fuselaje poco después del despegue, resultando en un accidente fatal para el piloto, quien era el único ocupante. La investigación reveló que el perno cónico inferior del ajuste principal del ala no estaba completamente enganchado durante el montaje, lo que llevó al fallo. El planeador fue destruido en el incidente, y se emitieron dos recomendaciones de seguridad como resultado de los hallazgos.

  1. Preflight assembly: On the morning of the accident, the pilot and friends rigged G-DBZZ for flight at Bicester Airfield, carefully consulting the Flight Manual as none of them had rigged this type before.
  2. Wing joint misrigged: During rigging, the lower bevel bolt of the wing main fitting did not fully engage with the lower lug stack of the main spar joint, leaving the primary wing attachment only partially secured and undetectably misrigged.
  3. Engagement not verifiable: The design of the wing main fitting allowed the pilots to complete the specified number of turns and feel little resistance, yet provided no means to verify full engagement of the lower bevel bolt.
  4. Pilot reassurance: After a first, uneventful but low winch launch during which the canopy opened, the pilot discussed the rigging and canopy issue with the owner by telephone and was reassured that the rigging had been done correctly.
  5. Winch launch - climb: On the second winch launch, the glider accelerated and rotated into a climb that some witnesses perceived as slightly fast and steep, remaining on the cable as it climbed through several hundred feet.
  6. Wing attachment failure: While still on the winch, the left wing bent upward about 20 degrees followed by the right wing, the lower bevel bolt failed, and both wings folded upwards and separated from the fuselage while remaining attached to each other at the main spar joint.
  7. Crash - fatal: With the wings detached, the fuselage pitched steeply nose-down and struck the ground, destroying the glider and fatally injuring the pilot.
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gliderincidents.com gathers and lists soaring incident reports from official sources. The sources are indicated and linked. These reports are amended by summaries, metadata and translations, some of which have been generated utilizing machine learning (AI). You shouldn't trust the information provided here blindly, and consider reading the official incident report as a fact-check.

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